Going to the dogs…..
http://www.theday.com/article/20101225/NWS01/312259946/1018
Security efforts Jacked up at L&M
By Judy Benson
Publication: The Day
New London, CT
http://www.theday.com/article/20101225/NWS01/312259946/1018
Security efforts Jacked up at L&M
By Judy Benson
Publication: The Day
New London, CT
Date: 12-26-2010 17:30
Program: Cal-Ore Life Flight
311 Cove Road
Brookings, OR 97415
541-469-7911
Type: Cessna 421C
Tail #: N31CU
Operator/Vendor: none
Team: Pilot, RN, Paramedic. No injuries reported. Patient on board.
Description:
The interfacility flight originated in Crescent City, CA (CEC), and
was destined for Medford, OR (MFR). The weather was IFR with marginal
VFR ceilings at both departure and destination, along with mountain
obscuration, rain and forecast light to moderate icing. All preflight
checks were normal, including deice equipment, and the risk assessment
matrix was within the acceptable range. The flight proceeded normally
with the pilot reporting some ice at 11,000′ in cruise, which was
easily removed with the deice equipment.
On descent into MFR, ice accumulation increased, and when leveling off
at approximately 8,000′, the pilot experienced a vibration followed by
the elevator control oscillations. Suspecting tail ice, the pilot
continued to select the deice boots. Though he confirmed the wing
boots were expanding and breaking off the ice, he did not get the
proper cockpit annunciation indicating that the tail was being deiced.
The pilot then confirmed a tailplane ice issue. The oscillations
continued on descent.
The pilot elected to declare an emergency and asked for vectors direct
to the airport. He was vectored to a lower and warmer altitude at
which time the ice begin to depart the aircraft and the elevator
control smoothed out. The pilot then accepted the ILS approach and
made a normal “no-flap” landing. The aircraft was met by the ground
ambulance and the patient was transported without incident. The
aircraft was taken out of service and all appropriate calls and
notifications made.
Additional Info:
Maintenance personnel have determined that a faulty pressure air line
in the deice boot had shifted, allowing expanded air to escape
overboard on the left vertical stabilizer deice boot edge. This
caused the tail deice boots to not inflate properly.
A follow-up discussion was conducted with all of the crew members and
personnel involved, and the incident is being referred to the QM
committee for review and comment.
Source: Dan Brattain, Program Director
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programs when an accident / incident has occurred. Please share the above
information with your program staff. If you have further questions, please
contact the CONCERN Coordinator, David Kearns at 800 525 3712 or email:
coordinator@concern-network.org.
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